I have a Felder KF700SP saw/shaper combo machine and the dust collection with the stock blade guard was insufficient. The stock guard has a very small port, maybe 1.5 I.D. I have been running a modified Felder guard where I heat formed a 3 plastic coupler to the Felder guard and I enlarged the opening of the guard itself. Collection was pretty good but I centered the plastic coupler so it ran straight vertically and the air clamps I use would sometimes hit the duct. Also the airflow was still less than ideal. The I.D. of the 3 coupler is 2.7 for a cross sectional area of 4.24. But, the enlarged opening of the Felder guard is only .9 by 3.3 for a cross sectional area of 2.97 which is about the area of 2 diameter port.
Here are pics of the original modified guard.
With the new modified guard I had two objectives; 1) increase airflow and 2) Improve clearance to the air clamps. I decided to use a 3 round to 7 by 1 (part #51026) nozzle that I purchased from Air Handling Systems. I sawed each corner about Ύ so I could bend tabs on the ends. I also trimmed them the match the profile of the top of the Felder guard and I drilled small holes for some self-tapping mounting screws.
Next I started cutting the top of the Felder guard out. First I cut the original 2 end off flush with the rest of the guard with a band saw. Then I used and air die grinder with a carbide burr to cut the rectangular slot. I ended up with a slot .9 by 6.5 long. That gives me a cross sectional area for the slot of 5.85. The I.D. of the 3 sheet metal adaptor is approx. 2.9 which is a cross sectional area of 6.6. So I didnt lose much in the transition from round to flat. Here are some pics of the guard after trimming.
I decided to attach the sheet metal transition to the Felder guard with small self-tapping screws and silicone adhesive. The screws really just held it in place while the adhesive set. Here are pics after mounting the transition.
The transition is mounted at a slight angle to keep the duct away from the air clamps on the slider. You can see that it tilts in one direction which is away from the slider. The transition is tall enough to clear the fence so it doesnt change how narrow I can rip. Here are pics of the guard mounted on the saw.
So now, how well did I achieve my two objectives? First the good news, I did improve the clearance for the air clamps. But the airflow measured with an anemometer in line with the 3 flex duct did not change. It measured approx. 6970 ft per min with both blade guard assemblies. I do use an Oneida Smart collector that speeds as CFM decreases up to utilize full HP of the system to generate the max possible pressure and therefore maximizing the CFM. Maybe the Smart collector is compensating? I can't see why the CFM did not change even though I almost doubled the cross sectional area of the port on the guard. Thoughts?...joe