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Thread: Motor Keyway Messed Up

  1. #31
    Quote Originally Posted by Jared Sankovich View Post
    From the pic its worn oversized (wallowed out) a lot. That chunk on the end looks like the original sidewall.

    Im guessing the key just falls out.

    I would personally weld it up and re-machine the keyway.
    Skip the welding and just cut another keyway 180º from the original

  2. #32
    Quote Originally Posted by Martin Wasner View Post
    Skip the welding and just cut another keyway 180º from the original
    Yup that's what the motor repair place said.

  3. #33
    Quote Originally Posted by Jared Sankovich View Post
    Its the g1023 saw, and likely will fit
    Sorry guys I missed this suggestion. That pulley is 7/8" bore and I need 3/4".

  4. #34
    Join Date
    Feb 2014
    Location
    Lake Gaston, Henrico, NC
    Posts
    9,029
    I didn't look through these for you, and I forgot what diameter you were looking for. I did a google search for 3/4" bore three groove pulley
    https://www.zoro.com/search?category...on%20Equipment

  5. #35
    Quote Originally Posted by Tom M King View Post
    I didn't look through these for you, and I forgot what diameter you were looking for. I did a google search for 3/4" bore three groove pulley
    https://www.zoro.com/search?category...on%20Equipment
    I just bought one on ebay for $35. Delta and other places wanted $70+.

  6. #36
    I had a damaged keyway on my tablesaw motor, the same issue as yours...
    I ended up welding and filing the damaged part, this took ages, as I'm not much of a welder.
    It was very difficult and the filing was slow, nitty gritty hard work on the fingers.
    I wouldn't want to do it again.
    worn keyway.jpg
    Having a guess, I'd say it most likely happened in the first place because the pulley was not drilled on center.
    I had to make a jig as I don't have a metal lathe... to mark file and scrape out the bore on center.
    I then made a bush/sleeve to fit into the pulley from a hunk of steel
    and turned it on the shaft of the motor.
    I then cut a keyway into my "new" pulley and made a key.
    In the end my key only fit 3/4 into the pulley/shaft and got stuck.
    I tried the "persuader" which led to me breaking some of my pulley...quite a lot of cursing happened.
    In the end I got the key out with quite a lot of careless angry bashes.
    The fit was so tooight that I didn't need a key
    So all that extra work of welding and filing the sides of the keyway, and making a key was a waste of time.

    Moral of the story...
    Check that pulley bore is on center
    file.jpgIMG_20170302_095859.jpgIMG_20170305_170945.jpgIMG_20170312_150328.jpgIMG_20170329_185102.jpgIMG_20170329_212003.jpg

    Still running perfect, admittedly I don't use the saw all that much.
    Good luck
    Tom

  7. #37
    Quote Originally Posted by Jared Sankovich View Post
    From the pic its worn oversized (wallowed out) a lot. That chunk on the end looks like the original sidewall.

    Im guessing the key just falls out.

    I would personally weld it up and re-machine the keyway.
    There it is! Perhaps you can measure things up and find a key that fits...

  8. #38
    Join Date
    Apr 2017
    Location
    Michigan
    Posts
    2,770
    Install a new key and lightly weld it to the shaft. First grind to make a little room for the weld.

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