Jeff Horton
04-08-2006, 6:07 PM
After adding the chuck to the J-Line I have discovered some runout in the spindle. Enough to be noticable. After some investigation I could track the runout all the way back to the nut on the spindle that the face plate and chuck register on.
Asked about this on the OWWM forum and someone suggested that 90% of the time the problem was with the nut not being true and suggested using a HSS steel scraper to true it up myself. I will skip some of the details but I used my parting tool to make very fine cuts on the nut. Looked like steel wool coming off the nut. I would dye it with a sharpie and brace the tool on the tool rest and the bed and every so slowly make my cuts using the blue as a guide to find the high spot and see what I had done.
Bottom line, it worked. I don't have a dial indicator but the runout has gone from very noticable to only noticable if you put something against the chuck while it is spinning. There is still some very minor runout. To correct this I am going to have to have to build a tool for this job because of the limited access to nut in the head stock. I think this will be close enough for woodworking tolerances. If not I will make a tool to finish truing it up.
Just wanted to pass this along incase someone else ran into something similar. This was so simple. Probably spent 15-20 minutes fixing the problem!
Asked about this on the OWWM forum and someone suggested that 90% of the time the problem was with the nut not being true and suggested using a HSS steel scraper to true it up myself. I will skip some of the details but I used my parting tool to make very fine cuts on the nut. Looked like steel wool coming off the nut. I would dye it with a sharpie and brace the tool on the tool rest and the bed and every so slowly make my cuts using the blue as a guide to find the high spot and see what I had done.
Bottom line, it worked. I don't have a dial indicator but the runout has gone from very noticable to only noticable if you put something against the chuck while it is spinning. There is still some very minor runout. To correct this I am going to have to have to build a tool for this job because of the limited access to nut in the head stock. I think this will be close enough for woodworking tolerances. If not I will make a tool to finish truing it up.
Just wanted to pass this along incase someone else ran into something similar. This was so simple. Probably spent 15-20 minutes fixing the problem!